70 lt1 leak down results - NCRS Discussion Boards

70 lt1 leak down results

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  • Dennis D.
    Extremely Frequent Poster
    • March 1, 2000
    • 1071

    70 lt1 leak down results

    Leak down with a cheap tester on a cold engine
    . Posted compression test last week and consistant with 1 at 180. Most at 190, and a couple at 195. This seems consistant as well, although crazy high leakage. All hissing coming from oil filler.Opinions?
    20191009_154408.jpg20191009_142902.jpg20191009_154507.jpg20191009_154257.jpg20191009_154323.jpg20191009_154343.jpg20191009_143439.jpg20191009_144417.jpg
    Compression results
    20191006_142731.jpg
  • Rich G.
    Extremely Frequent Poster
    • August 31, 2002
    • 1396

    #2
    1966 L79 Convertible. Milano Maroon
    1968 L71 Coupe. Rally Red (Sold 6/21)
    1963 Corvair Monza Convertible

    Comment

    • Dennis D.
      Extremely Frequent Poster
      • March 1, 2000
      • 1071

      #3
      Re: 70 lt1 leak down results

      Thanks Rich. If I'm understanding you, I put 90# in , then zero out the percent gauge before connecting to cylinder.

      Comment

      • Rich G.
        Extremely Frequent Poster
        • August 31, 2002
        • 1396

        #4
        1966 L79 Convertible. Milano Maroon
        1968 L71 Coupe. Rally Red (Sold 6/21)
        1963 Corvair Monza Convertible

        Comment

        • Dennis D.
          Extremely Frequent Poster
          • March 1, 2000
          • 1071

          #5
          Re: 70 lt1 leak down results

          Originally posted by Rich Giannotti (38594)
          Dennis

          on my gauge we set 80# on the input side and with the output side blocked with the the shut off in the off position the other gauge should read 80#. That would be 100%. Then connect to the cylinder while your friend holds the propeller at TDC for that cylinder. Then turn the valve on and the second gauge reads what’s being held. Numbers in the mid 70’s are good. 64 is minimum. Sometimes we touch up the input to keep it at 80#. Also we have the advantage of being able “rock” the prop a bit to get exactly TDC which is difficult in a car.

          matbe that’s a different unit which I’m not familiar with, so let’s wait and see what somebody more experienced says.

          Rich
          So someone suggested I modify the tester I have and get rid of the % gauge. I moved the pressure gauge to the vacated spot and plugged the first port. I now have a gauge I can pressure with 100#, then plug into a cylinder and read the pressure difference. I think this is the setup you were explaining.

          I retested cylinder 5,(since that was where the balancer was last set. The new setup showed 9% on the same cold engine instead of the 50% I had before. Ill probably retest the rest, but Im feeling good they will be similar.
          Here's a pic of the original #5....
          Attached Files

          Comment

          • Dennis D.
            Extremely Frequent Poster
            • March 1, 2000
            • 1071

            #6
            Re: 70 lt1 leak down results

            New results with modified gauge set at 100# inlet. Compression is great. These numbers seem quite good as well. Up until now I haven't really disturbed anything. Wondering if I should remove valve covers to check seal. Not sure I can check guides with just removing valve covers. Also wondering if I should adjust the valves since I still have the balancer taped in 90 degree increments. All part of the while i'm at it senario.

            Attached Files

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            • Patrick B.
              Extremely Frequent Poster
              • August 31, 1985
              • 1986

              #7

              Comment

              • Rich G.
                Extremely Frequent Poster
                • August 31, 2002
                • 1396

                #8
                Re: 70 lt1 leak down results

                Dennis

                Thats more like it!

                Rich.
                1966 L79 Convertible. Milano Maroon
                1968 L71 Coupe. Rally Red (Sold 6/21)
                1963 Corvair Monza Convertible

                Comment

                • Bob I.
                  Very Frequent User
                  • November 9, 2006
                  • 265

                  #9

                  Comment

                  • Dennis D.
                    Extremely Frequent Poster
                    • March 1, 2000
                    • 1071

                    #10
                    Re: 70 lt1 leak down results

                    Thanks Patrick. I don't know when the valves were done. But judging from other things I've found, I'm not that confident the previous owner did it correctly. Will just be another item off my list.

                    Rich. I thought you'd relate to my second testing. Makes more sense.

                    Comment

                    • Dennis D.
                      Extremely Frequent Poster
                      • March 1, 2000
                      • 1071

                      #11
                      Re: 70 lt1 leak down results

                      Hey Bob How are you. All the air is coming from the valve covers. Very faint. Not leaking anywhere else. Assuming its normal air passing the rings, being the compression and leakdown are looking good.

                      Comment

                      • Richard G.
                        Extremely Frequent Poster
                        • July 31, 1984
                        • 1715

                        #12
                        Re: 70 lt1 leak down results

                        How did you hold the motor at TDC?
                        That has always been the issue when I preform this test.

                        Comment

                        • Dennis D.
                          Extremely Frequent Poster
                          • March 1, 2000
                          • 1071

                          #13
                          Re: 70 lt1 leak down results

                          Originally posted by Richard Geier (7745)
                          How did you hold the motor at TDC?
                          That has always been the issue when I preform this test.
                          I got lucky with taping the balancer. I did it in 4 segments and each cylinder seemed dead on tdc. That's why I'm thinking to leave it on and check the valves.

                          Comment

                          • Bob I.
                            Very Frequent User
                            • November 9, 2006
                            • 265

                            #14
                            Re: 70 lt1 leak down results

                            Originally posted by Richard Geier (7745)
                            How did you hold the motor at TDC?
                            That has always been the issue when I preform this test.
                            Sometimes the piston will moved during the test. Were wondering if you experienced that during your testing. If you do, leaving the other plugs in helps.

                            Comment

                            • Richard G.
                              Extremely Frequent Poster
                              • July 31, 1984
                              • 1715

                              #15
                              Re: 70 lt1 leak down results

                              Next time I will do both, index the balancer and do one plug at a time.
                              In my experience if I was off only a skosh the air pressure would rotate the motor.
                              Thanks for the tips. I really enjoy this site.
                              Rick

                              Comment

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