1967 Headlamp Switch Repair & Testing, and some Interesting Observations - NCRS Discussion Boards

1967 Headlamp Switch Repair & Testing, and some Interesting Observations

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  • Richard M.
    Super Moderator
    • August 31, 1988
    • 11302

    1967 Headlamp Switch Repair & Testing, and some Interesting Observations

    Last week a friend who was working on his 1967 had two 1995131 Headlamp switches that didn't dim the cluster lamps, only full bright. We diagnosed the faults using his voltmeter, probing the switch terminals as I walked him through some tests by phone. Both rheostats were bad.

    I had a old 1995149 Headlamp switch sitting on the shelf, along with many other old original switches that have been waiting for me to repair. I knew it had a bad rheostat, so I decided to experiment.
    1203221742_resized.jpg

    I took the 149 switch apart and saw it had a break in the rheostat close to the rivet where it terminates. All rheostats typically break in this area due to the arcing when coming off of the the rivet, which is the load from the lamps. As I recall, the rheostat wire is made of tungsten and difficult to repair. I used needle nose pliers and removed the broken piece and left a small piece still attached to the rivet.

    Then I stretched to remaining wire over toward the rivet and the remaining wire. Using a high heat soldering iron, liquid flux, and silver solder, I was able to repair it. I gave it the tug test with a pick and it appeared strong. I later tested the repair electrically, using a 1967 Main harness loaded with dash bulbs. Results described later, along with some interesting observations.

    So I attempted to also fix the two 131 switches using a similar repair method. Here are some photos of the repair sequence. I took photos this time. Note the photos may be from either switch, as evidenced by the two colors of the plastic actuator.

    Using a flat blade screwdriver, lift the metal tabs away from the housing. Carefully lift the metal cover away from the housing.

    After disassembly, you can see the rheostat wire broken close to the rivet. All switches usually have this fault. It was the weak link in the design. The heat generated nears 300*F when in it's lowest voltage setting, which is approximately 6 volts when fully dimmed, i.e. switch knob fully clockwise before the "off" position.
    1204221248_resized.jpg


    1204221248a_resized.jpg

    After removing the short piece, I stretched the wire over to the remaining wire clamped by the rivet. Using the silver solder they were now reconnected. The rheostat resistance is approximately 6 ohms. The short piece I removed is negligible, likely a few hundred milliohms.
    1204221302b_resized.jpg

    1204221303_resized.jpg

    I cleaned the rivets and verified good contact to the wire. If needed I could also solder the wire to the rivet. I actually repaired the 149 switch using that method.

    The other 131 switch was taken apart further by the owner. I also soldered the backside of the rivets to the terminals.
    1203221717_resized.jpg

    I also soldered the terminals back to the contact plate within the switch housing after assembly as shown below.
    1203221819_resized.jpg

    I reassembled the switch after cleaning all contacts and using a silicone grease on the moving parts, note not on the contact points. The most difficult part of the process is keeping the contact block oriented properly. The end of the contact block with the hole for the knob shaft tip faces the knob. The o-ring is used to hold the contact block in place during reassembly.
    1204221154_resized.jpg

    The rheostat contactor wheel center hole mates only one way with the plastic actuator shaft. The spring attaches over the plastic actuator shaft first, then the wheel, ensuring the contactors face the rheostat. The spring keeps pressure on the contactor wheel to the rheostat.
    1204221158_resized.jpg


    1204221158a_resized.jpg

    Note that earlier switches used a solid contactor wheel without the "fan" blades like on these later designs. Research explained the slotted fan blades were incorporated to help reduce heat, acting as a heat sink with multiple cooling features.

    Here it is preassembled using the o-ring to hold the contactor assembly. Note the plate on top of the contactor(shown in a previous photo). A spring underneath it keeps it tensioned. The end of the plate has a keyhole which is used to capture the tip of the knob shaft. When the outer small button on the metal plate cover of the switch is pressed, it presses down on the plate/spring, lowering the plate to allow shaft removal.
    1203221759_resized.jpg

    Place the wheel/actuator assembly into the center hole in the rheostat porcelain and hold with one hand. Now the metal cover can be reinstalled with the other hand, simultaneously placing the front of the metal cover over the plastic actuator, then over the porcelain and down over the housing. At this point slide the o-ring away while keeping the assembly tight. Using a flat blade screwdriver, press the metal tabs of the cover back over the housing side keepers.
    1204221202_resized.jpg

    1203221818a_resized.jpg

    So I had to test all 3 switches for functionality. I used a ohm meter to check all switch functions, including the dimming function. The rheostat measures around 5 ohms, rivet end to end of coil.

    All tests passed. I then configured a main harness loaded with dash bulbs. I had to jumper each lamp socket ground as I didn't have a cluster. I left each switch in full dim mode for about 10 minutes. All 3 switches had fully functional rheostats again.
    Note that to save the life of the rheostat, keep the lamps on bright. By design, this bypasses the rheostat from the circuit

    Full Bright
    1205221415_resized.jpg

    Dimmed
    1205221405_resized.jpg

    Full Bright in darkspace
    1205221414_resized.jpg

    Dimmed in darkspace.
    1205221415a_resized.jpg

    Are you noticing that the lamps closest to the voltage source, left side, are brighter than those farther away at the clock area to the right?
    I believe this is a artifact of the harness design. From the fuse panel, only one 18 Gauge Gray wire enters the harness and feeds all 14+ dash lamps. The furthest lamps get slightly lower voltage due to the voltage drops along the harness.

    Another interesting measurement. Be very careful when putting hands up on a operating switch when in dimming mode. Also make sure all wires and loose items are far away from the switch.

    The housing.....267*
    1205221412_resized.jpg

    The porcelain....279*. Note at one instant it read 288*.
    1205221413_Burst01_resized.jpg

    EDIT: 2/15/2024

    NEVER USE ANY TYPE OF LUBRICANT, PARTICULARLY ANYTHING FLAMABLE, ON THE RHEOSTAT!!! IF IT SQUEAKS, IT'S NORMAL.

    Notes:

    The wheel contactor outer contact rivet is the source voltage from the fuse panel Tail lamps circuit. The wheel center contact goes to the lamps, via a fuse. This functions only when the knob is pulled in Park or Headlamp mode. Note that because of this design feature, if you ever notice dash lamps off, it could be the main fuse for the tail lamp circuit is blown, a dangerous driving condition.

    Rotating knob positions are as follows:

    Full CW - Dash lamps Off
    In this position the rotating wheel outer contactor moves away from the rheostat wire on to the porcelain, opening the circuit.


    Full CCW(before detent click) - Dash lamps Full bright
    In this position the rotating wheel contactor moves away from the rheostat wire on to the rivet supplying max voltage to the lamps.


    Full CCW(after detent click) - Dash lamps Full bright, Courtesy lamps On
    In this position, as above, the dash lamps are still full bright, and a separate copper contactor is closed onto the switch metal cover, activated by the plastic actuator tab pushing down on the copper. This connects cluster ground to the separate courtesy lamp circuit, turning them on.


    Partial rotation CW/CCW - Dash lamps Dimmed CW, Brighter CCW
    The rheostat is in the circuit varying voltage to the lamps.

    ====
  • Dan D.
    Extremely Frequent Poster
    • November 5, 2008
    • 1323

    #2
    Re: 1967 Headlamp Switch Repair & Testing, and some Interesting Observations

    Hi Rich,

    I have repaired several of these switches for other NCRS members. I have a couple of comments for you.

    1. I have found the rivet can get so corroded it blocks all conductivity. Dis-similar metal syndrome. I have drilled the rivet out and replaced it with a #4-40 stainless screw and nut. Yours looks corroded pretty bad, but apparently it still works.

    2. I use Dow Corning Molykote Gn paste for grease. This is a boundary lubricant in a mineral oil base and will not destroy conductivity like silicone lubricants will (not an dielectric). You can apply it to the rheostat wire, it will not destroy electrical contact but it lowers the friction between the rheostat wire and the rotating contact block. Burnish the stuff in by rubbing it in with a lint free rag. It is speced at 250*F, but I don't see this as a problem. This stuff can also be used as a anti-seize lubricant for assembling bolts/nuts, but you have to reduce the torque as it lowers thread friction substantially.

    3. Interesting use of an o-ring. I have been using a tie-wrap, but it is difficult to tighten a tie-wrap with one hand. I like your idea better.

    Very good article Rich, very detailed and accurate.

    Dannnn

    Comment

    • Richard M.
      Super Moderator
      • August 31, 1988
      • 11302

      #3
      Re: 1967 Headlamp Switch Repair & Testing, and some Interesting Observations

      Dan, I was hoping to get some thoughts from you on this.

      Yes I actually cleaned and soldered some of the rivets on the backside, and on that 149 I soldered the wire directly to the rivet to guarantee contact. I added a few more photos to the post.

      Hopefully this method will last. Silver solder has a melting point of around 400*F so I believe it should work well.

      Good info regarding the Molykote grease. I'll look for some.

      Thanks for the feedback,
      Rich

      Comment

      • James G.
        Very Frequent User
        • August 22, 2018
        • 783

        #4
        Re: 1967 Headlamp Switch Repair & Testing, and some Interesting Observations

        Good to know on the Molycote.
        For the past 10-15 years I have been using NOALOX.
        Electrical joint compound for bi-metallic electrical connections, it is supposed to prevent galvanic corrosion.
        If I pull something electrical in the shop, it will have this on the contacts when I put it back together. Steering column starter switches, clutch safety - In every harness connection, and on grounds.
        100_9577.jpg
        James A Groome
        1971 LT1 11130 - https://photos.app.goo.gl/zSoFz24JMPXw5Ffi9 - the black LT1
        1971 LT1 21783 - 3 STAR Preservation.- https://photos.app.goo.gl/wMRDJgmyDyAwc9Nh8 - Brandshatch Green LT1
        My first gen Camaro research http://www.camaros.org/forum/index.p...owposts;u=4337
        Posts on Yenko boards... https://www.yenko.net/forum/search.php?searchid=826453

        Comment

        • Dan B.
          Expired
          • July 13, 2011
          • 545

          #5
          Re: 1967 Headlamp Switch Repair & Testing, and some Interesting Observations

          Richard, Very nice write up with your usual great detail , thanks for posting this for us. I've not had to do this repair yet, but would not hesitate to try it now. Cheers!

          Comment

          • Richard M.
            Super Moderator
            • August 31, 1988
            • 11302

            #6
            Re: 1967 Headlamp Switch Repair & Testing, and some Interesting Observations

            Thanks Dan. BTW, in a recent thread from last week....Here....

            I linked that into this thread for reference.

            There's a PDF of that C1 HL Switch repair thread that Ed Z extracted from it some time ago, that he then transferred to a DOCX, then Jack M converted to a PDF.

            It's in the Sticky "DoRD", Update Page, so you can download and save for future reference.

            This one....
            Headlight_Switch_Repair_Rev2.2.pdf

            I'll check in with my HTML to PDF conversion experts and maybe get this C2 version thread written up too.

            Rich

            Comment

            • Ronald L.
              Extremely Frequent Poster
              • October 18, 2009
              • 3248

              #7

              Comment

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